  
									
									
									
										
                                           
									 
									
										
                                        This page will be a running account of 
                                        progress on the Scout. 
									
										
                                        Last 
                                        updated:
                                        04/05/2010 
									
										  
									
										March 
                                        27-28, 
                                        2010  
									
										Attended the  
                                        AZIHR again this year. Got another first 
                                        place and ran the Hassyampa River. 
									
										Since I'm 
                                        only doing maintenance on the SR-2 now, 
                                        I won't post up anything more unless I 
                                        do some significant upgrades or changes. 
									
										  
									
										March 28, 
                                        2009  
									
										Attended the
                                        
                                        AZIHR in Wickenburg, AZ. Got a first 
                                        place for Mild Scout 800s and went on a 
                                        trail run up the
                                        
                                        Hassyampa River. 
									
										  
									
										November 16, 2008 
									
										After the 
                                        trip to 
                                        RMIHR, where I took a second 
                                        place for Mild Modified Scout 800s, I 
                                        went on a trail run to the
                                        
                                        San Francisco River in eastern 
                                        Arizona with the Sonora Desert Scouts 
                                        club. 
									
										  
									
										July 12, 
                                        2008 
									
										Got 
                                        everything reassembled and finished 
                                        applying the rocker and beltline vinyl 
                                        stripes. All ready for RMIHR!  
									
										
                                          
									
										  
									
										  
									
										July 6, 2008 
									
										Shot the 
                                        finish coat on the body. There's less 
                                        than 2 weeks before we leave for RMIHR. 
                                        Gotta get everything back together and 
                                        apply the stripes. 
									
										  
									
										
                                          
									
										  
									
										  
									
										  
									
										  
									
										  
									
										  
									
										  
									
										  
									
										  
									
										  
									
										  
									
										  
									
										July 5, 
                                        2008  
									
										I laid out 
                                        the hood graphic and masked it off. I 
                                        used rattle can white Rustoleum enamel. 
                                        The graphic is not strictly to the 
                                        dimensions of the original SR-2 appliqué 
                                        but it looks good enough for a 
                                        10-footer!  
									
										  
									
										                                                   The body is 
                                        prepped and primered and ready for the 
                                        finish coat. 
									
										  
									
										  
									
										  
									
										  
									
										  
									
										June 29, 2008 
									
										
                                        
                                         I removed 
                                        the hood and nosepiece from the Scout 
                                        and set the hood up for painting so I 
                                        would be shooting a vertical surface. 
                                        After 3 coats of primer, I cleaned the 
                                        HVLP gun and mixed up a batch of IH 
                                        Flame Red. Somehow, I managed to loose 
                                        the spring that puts tension on the flow 
                                        control rod which rendered the HPVL gun 
                                        useless. Not wanting to waste a batch of 
                                        paint, I brought my 10 year old 
                                        Craftsman siphon paint gun out of 
                                        retirement and shot the hood and 
                                        nosepiece. Much more overspray than with 
                                        the HPLV! I now have a nice re-orange 
                                        garage floor. 
									
										  
									
										  
									
										June 21, 2008  
									
										Shot the 
                                        color on the top today. It came out very 
                                        nice except for a few sags here and 
                                        there. This was just the right sized 
                                        project to help me get familiar with the 
                                        gun and polish my spraying technique a 
                                        little before I tackle the body. I'll let 
                                        it dry overnight and sand out the sags 
                                        and some of the rougher orange peel 
                                        tomorrow. It was surprising that the 
                                        color of the Alpine White was not as 
                                        white as I expected. I guess 37 years in 
                                        the sun bleached the old paint out a 
                                        little. 
									
										  
									
										June 14, 2008  
									
										
                                        
                                         Now 
                                        that the transmission is back in and 
                                        seemingly working well, I've finally 
                                        turned my attention to the repaint. I 
                                        removed the top and sanded the scratches 
                                        and filled some small dents. I applied 
                                        three coats of primer with a HVLP spray 
                                        gun from Harbor Freight and am now ready 
                                        to shoot the color coat of I.H. Alpine White. 
									
										  
									
										  
									
										  
									
										  
									
										April 16, 2008  
									      
                                            For the 
                                            last 2 weeks, I've been working on 
                                            replacing the transmission. I 
                                            acquired a Borg Warner 12 automatic 
                                            from another Scout that had swapped 
                                            in a  
                                            T19. I had the transmission rebuilt 
                                            by a commercial shop using all new 
                                            parts and a rebuilt torque 
                                            converter. During the time the 
                                            transmission was out, I took the 
                                            opportunity to replace the rear 
                                            engine block freeze plugs and reseal 
                                            the oil pan and replace the rear 
                                            main bearing cap side seals. 
                                            Hopefully, this will reduce the 
                                            amount of oil that has previously 
                                            leaked from my Scout. 
                                            Once the transmission was back from 
                                            the shop, a friend and I installed 
                                            it in a couple of hours. It took 
                                            another few hours to hook the front 
                                            drive shaft up with new U-joints and 
                                            get the transmission cross member 
                                            back in place. 
                                            I still need to hoo k 
                                            up the water hoses to the 
                                            transmission heat exchanger, hook up 
                                            the rear drive shaft and reinstall 
                                            the shifter.   
									
										
										March, 2008 
                                        Well, it's been a whole year since I've 
                                        updated the progress page. I've been 
                                        having too much fun driving and wheeling 
                                        the Scout to take any time to work on 
                                        it! I finally decided to go ahead and 
                                        repaint this year. I started by filling 
                                        dents and sanding out scratches on the 
                                        sides. Once I get the front and rear 
                                        done I can remove the top and shoot a 
                                        new coat of paint on. 
									
										  
									
										
										March, 2007 
                                        The SR-2 has been running great for the 
                                        few times I've driven it this year. I 
                                        went on a trail run with the Sonora 
                                        Desert Scouts on Feb 24 and it performed 
                                        beautifully! So much so that I hesitate 
                                        to run it off road too much more for 
                                        fear of turning it into a beater trail 
                                        rig. Just so happens I have a candidate 
                                        for that job. A 1971 800B that I picked 
                                        up cheap to use as a parts truck turns 
                                        out to be a worthy candidate for a trail 
                                        rig. It's got a 196 I4 with a T-18 and 
                                        Dana 20 and a PTO winch! The body is 
                                        already beat up so I won't have to worry 
                                        about taking it on any type of trail. So 
                                        now, I'm splitting time between working 
                                        on my 
                                        Comanche restoration and getting 
                                        some things checked out on the trail 
                                        Scout. I'm still planning to do a paint 
                                        job on the SR-2 before attending the 
                                        RMIHR in July. 
									
										  
									
										
                                        August 1, 2006  
                                        Wow! It's hard to believe it's been a 
                                        year since I posted an update. The 
                                        Scout's been running pretty good. I take 
                                        it out once a month to the Sonora Desert 
                                        Scouts meeting and drive it to work 
                                        every other week. I've been busy working 
                                        on my new garage which is almost 
                                        finished and ready to start working in. 
                                        I've also acquired a couple of parts 
                                        Scouts. 
                                           
									
										There was no 
                                        AZIHR this year 
                                         and I didn't get to go 
                                        to the Rocky Mountain Rendezvous either.
                                         
									
										  
									
										
                                        August 7, 2005 
                                           Not too 
                                        much to report since the last update. I 
                                        dropped the 
                                         Borg 
                                        Warner transmission pan and cleaned the 
                                        filter screen. I replaced the filter and 
                                        filled the trans with new Dexron III per 
                                        the shop manual instructions. I used a 
                                        gasket in the Fram FT1024  kit from 
                                        Rock Auto. Now the trans leaks like a 
                                        seive! I've tightened the bolts down a 
                                        couple of times but it's still leaking. 
                                        I guess I'll have to drop it again and 
                                        use some Right Stuff on it. 
									
										We went to 
                                        the Rocky Mountain IH Rendezvous in 
                                        July. I had some problems with the 
                                        Holley 2300 flooding out so I couldn't 
                                        go on the Monday trail run. I replaced 
                                        the float bowl valve and it seemed to 
                                        fix the problem. We did some back road 
                                        cruising at my son's place in Orderville, 
                                        UT after the Rendezvous. During the 
                                        trip, one of the wires from the ignition 
                                        switch broke off the starter solenoid. 
                                        We did a trail fix to get it going 
                                        again. I guess some wiring repairs will 
                                        be next on my list.  
                                          
                                          May 14, 2005 
                                           I finally 
                                          got around to installing the new turn 
                                          signal harness I had purchased form 
                                          Shee-Mar, Inc. back in  October. 
                                          I had  
                                          continued to have problems with my 
                                          stop lights since I messed with 
                                          replacing the switch shortly after I 
                                          got the Scout. Only on brake light 
                                          would come on unless the turn signals 
                                          were activated. I set aside most of 
                                          the day to R&R the harness. Removing 
                                          the old one went pretty fast. Once I 
                                          got the steering wheel off and removed 
                                          the screws holding in the T/S switch 
                                          and hazard switch, I noted the 
                                          location of the 6 conductor harness 
                                          connector and verified that the new 
                                          harness matched up, I was ready to 
                                          remove it. I took a while to get the 
                                          connector pried apart without breaking 
                                          anything. Since I wasn't going to 
                                          re-use the old harness, I cut the 
                                          wires off at the switches and pulled 
                                          the harness out of the column. Then, I 
                                          removed the terminals from the 
                                          connector shell. I fished the wires 
                                          from the new harness back through the 
                                          column. It was easier to fish them 
                                          with multiple fish wires attached to 2 
                                          or 3 wires rather than try to pull 
                                          them all through at once. I got the 
                                          new wire terminals plugged into the 
                                          old connector shell and re-attached 
                                          the switches. Of course despite having 
                                          made myself a diagram before I 
                                          disassembled the connector, I still 
                                          managed to switch the brown and green 
                                          wires. So when I tested the turn 
                                          signals, the left turn postion flashed 
                                          the right tail light and vise-versa. 
                                          After swapping the wires back to where 
                                          they belonged, everything worked fine. 
                                          Now I have turn signals with BOTH 
                                          lights!  
                                          
                                          April 9-10, 2005 
                                           My annual 
                                          trip to Prescott Valley for the 
                                          Arizona IH Rendezvous. 
                                          
                                          March 12, 2005 
                                           Installed 
                                          the rear liftgate and tailgate seal I 
                                          got on Ebay today. This was original 
                                          IH weatherstrip PN 374441C1 so it fit 
                                          perfectly. I paid $50 for it which I 
                                          thought was resonable since the 
                                          comparable aftermarket molding from 
                                          Metro Molded Products (PN LP 103-G) 
                                          sells for about $2.50/ft and it takes 
                                          11 feet.  I still need a piece to 
                                          go on the bottom edge of the liftgate 
                                          so I may order it from them. 
                                          
                                          February
                                          12, 2005 
                                           After I 
                                          got the top back on, I decided I 
                                          should finally install the door 
                                          weatherstrip I got from ScoutParts.com 
                                          about a year ago. I removed the old, 
                                          dried and cracked original seals and 
                                          wire brushed the loose particles off. 
                                          Then, I used some Xylene to soften and 
                                          remove the remaining adhesive. I 
                                          installed the new seals with GM 
                                          Weatherstrip Adhesive. Because the 
                                          windows don't end up in the correct 
                                          place when rolled up and the doors 
                                          still have a bit of sag, the windows 
                                          don't seal tight against the new 
                                          gaskets. I'll have to do some playing 
                                          with the adjustments on the doors and 
                                          windows to get a better seal. 
                                          
                                          December 2 8-31, 2004 
                                           I took 
                                          advantage of a week off from work 
                                          during the Holida ys 
                                          to finish up the floor project. Got 
                                          two coats of orange Durabak 18 bed 
                                          liner layed down. The color is pretty 
                                          close to the original Omaha Orange on 
                                          the Scout but I expect it to fade as 
                                          it ages. If it gets too "pinkish", 
                                          I'll have to top coat it with some 
                                          orange enamel. Anyhow, once the bed 
                                          liner cured for a couple of days, I 
                                          put the roll bar in and then put the 
                                          gas tanks in. After re-attaching the 
                                          front seats, I fired her up and took a 
                                          short trip to the gas station to top 
                                          off one of the tanks. Sure felt good 
                                          to have her back on the road!. Now 
                                          it's time to put the travel top back 
                                          on for a couple of our winter months. 
                                          
                                          December 19, 2004 
                                           Finally 
                                          got an entire weekend to work on the 
                                          Scout so I took advantage of the 
                                          sunshine and low 70's weather to 
                                          complete the floor pan installation. A fter 
                                          some more minor grinding and 
                                          adjustments, the pan fit into place. I 
                                          placed 3/16" pop rivets in several 
                                          locations to hold it in place and then 
                                          put spot MIG welds around the 
                                          perimeter. I put a few underneath also 
                                          wherever I could reach and there 
                                          wasn't an exhaust pipe or frame rail 
                                          in the way. After a while, some of the 
                                          welds actually looked pretty good! 
                                          Then I ran  bead of seam sealer 
                                          around the edges of all the seams to 
                                          keep out water.  I welded in the 
                                          seat base I had gotten a couple months 
                                          ago which was the start of this whole 
                                          project. After Christmas, I'll lay 
                                          down a double coat of bed liner and 
                                          then I can start putting things back 
                                          together. 
                                          
                                          December 
                                          12, 2004 
                                           The new 
                                          floor panel arrived so I set about 
                                          doing the prep work to get it ready to 
                                          go in the Scout. Although it was cut 
                                          to the correct shape, I had to do  
                                          some minor grinding to get it to fit 
                                          properly. Then I cut out the holes for 
                                          the drain plug, gas tank selector 
                                          valve, body mount bolt and gas pedal 
                                          studs. Next, I welded the braces to 
                                          the underside of the panel. I also 
                                          repaired the gas line I cut when 
                                          removing the old floor. Everything is 
                                          pretty much ready to go back in now. 
                                          If the weather is nice next weekend, I 
                                          should be able to get this part 
                                          finished. The Scout looks pretty sad 
                                          sitting there with no top, seats or 
                                          roll bar and the rear wheels off.  
                                          
                                          
                                           November 25, 2004 
                                           While the 
                                          Thanksgiving turkey was cooking, I 
                                          took the opportunity of being home 
                                          from work to clean up the areas where 
                                          the new floor will be attached.  
                                          I also removed, straightened and 
                                          cleaned up the braces and spacer from 
                                          the old floor pan. These will need to 
                                          be reattached to the new panel before 
                                          it gets welded in place. The floor 
                                          panel I ordered from
                                          
                                          ScoutParts.com hasn't come yet. 
                                          Apparently, there was a problem with 
                                          steel supply at the manufacturer. 
                                          That's just as well as it gives me 
                                          time to prepare all the little things 
                                          that need to be done before the floor 
                                          goes in. Hopefully, I'll be able to 
                                          get the floor back in next weekend. 
                                          After that, I can resume my original 
                                          project: coating the bed and floors 
                                          with bed liner. 
                                          
                                          November 20, 2004 
                                           I've 
                                          spent the last two weekends
                                          
                                           cutting 
                                          out the old floor panel. It involved a 
                                          lot of drilling out spot welds and 
                                          using an air chisel to finish 
                                          separating the sheet metal from the 
                                          rest of the Scout. I ended up cutting 
                                          out sections of floor to make it 
                                          easier to access some of the spot 
                                          welds. I salvaged the channel braces 
                                          from the underside of the floor and 
                                          will need to practice my MIG welding a 
                                          little to get those attached to the 
                                          new floor.. 
                                          
                                          November 
                                          6, 2004 
                                           As is 
                                          typical when working on Scouts, I got 
                                          an unpleasant surprise from the rust 
                                          monster. I removed the front driver's 
                                          seat base thinking that the underlying 
                                          floor sheet metal was fairly solid. 
                                          Once the seat base was removed, the 
                                          rust situation was worse than 
                                          originally thought. There are several 
                                          rust-through areas that were hidden by 
                                          the seat base flanges that were spot 
                                          welded to the floor. In order to 
                                          insure a solid support for the new 
                                          seat base, it's going to be necessary 
                                          to replace the entire driver's side 
                                          floor. So now I will have to remove 
                                          the roll bar, one body mount bolt and 
                                          the gas pedal ball studs, then drill 
                                          out the spot welds and air chisel the 
                                          floor panel out. Fortunately, 
                                          replacement floor sheet metal is 
                                          available for the 800. I might also 
                                          take this opportunity to install some 
                                          mounts for the roll bar that are 
                                          attached to the frame. 
                                          
                                          October 24,
                                          2004 
                                           I thought 
                                          it was going to be a simple job to 
                                          remove the seats, old floor  
                                          mat and apply rust encapsulator to the 
                                          front floor. After pulling up the mat 
                                          and scraping off the rubber sound 
                                          deadening/insulation, I discovered 
                                          that the driver's seat base was pretty 
                                          badly rusted away. The floor panels 
                                          themselves have some pitting but are 
                                          basically solid. Before I finish 
                                          applying the Rust Bullet and then the 
                                          DuraBak, I've got to remove the old 
                                          seat base and weld in a new one. I 
                                          also discovered some weak metal in the 
                                          floors under the front mount plates 
                                          for the roll bar. This will have to be 
                                          dealt with eventually. I will probably 
                                          make some 3/16 brackets to bolt on 
                                          underneath and weld on to the frame.   
                                          
                                          October 17, 
                                          2004 
                                           While the 
                                          travel top was still off the truck, I 
                                          took the opportunity to do some work 
                                          on the rear bed. I had pulled up the 
                                          rubber mat a couple of months ago and 
                                          scraped off the rubber membrane 
                                          underneath. There were some pretty 
                                          severe rust  spots, especially 
                                          along the edges where the bed meets 
                                          the side panels. There was lots of 
                                          pitting and a couple of pin holes all 
                                          the way through. I wire brushed all 
                                          the loose rust scales off, filled the 
                                          pin holes with body filler, cleaned 
                                          with some High Efficiency Reducer 
                                          (which is mostly xylene) and applied 
                                          two coats of
                                          
                                          Rust Bullet rust 
                                          prevention/control product. It's a 
                                          thinner consistency than Eastwood's 
                                          Rust Preventer put as it cures, it 
                                          becomes thicker. Before the top goes 
                                          back on for the winter, I'll coat the 
                                          floor with some
                                          
                                          DuraBak textured bed liner to 
                                          further water proof it and cover the 
                                          rust pits. It comes in colors so I'll 
                                          do it with orange to match the rest of 
                                          the Scout. 
                                          
                                          August 22, 2004 
                                           Decided
                                          to put in the passenger side window
                                          regulator I got to replace my old one
                                          which binds up pretty bad. I thought
                                          it was because the arms might be bent
                                          but for sure the two missing mounting
                                          screw posts didn't help. While I was
                                          at it I installed new window "felts"
                                          (anti-rattle strips) from Anything
                                          Scout. The strips are  not exact
                                          replacements for the Scout 80/800.
                                          They are rubber "wipers" on
                                          both sides and have no chrome bead
                                          like the originals. No big deal but
                                          the bigger issue was that the holes
                                          for the mounting clips are not in the
                                          same locations as the original. This
                                          was not going to be  a quick, snap
                                          out-snap in replacement. I decided to
                                          mark the new locations and drill holes
                                          for some #8 self tapping sheet metal
                                          screws. On the inside, I used some 
                                          window belt weatherstrip from 
                                          Restoration Specialties (P/N M113) 
                                          which is a close replacement for the 
                                          original. Those pieces are attached 
                                          with wire staples and require some 
                                          drilling and tedious replacement of 
                                          the new staples to get them installed. 
                                          A quicker way would be to use 1/8" pop 
                                          rivets which would be buried deep 
                                          enough in the fuzzy pile and not 
                                          scrape against the window.  The 
                                          rear edge window guides were replaced 
                                          with felt window channel from 
                                          Restoration Specialties (P/N 10-E-60). I got 
                                          everything in but the window still doesn't 
                                          work perfectly. I still have
                                          to pull it by hand to get it to roll
                                          all the way up. And going down, it
                                          seems to hit something that keeps it
                                          from lowering smoothly. I have to let
                                          it fall hard against the resistance to
                                          make it go down past whatever the
                                          restriction is. Oh well. At least I
                                          got the felts put in so the window
                                          doesn't rattle anymore. It makes a big 
                                          difference when driving on rough 
                                          roads, even around town. 
                                          
                                          
                                           August 
                                          7, 2004 
                                           I 
                                          got the new seat covers back from the 
                                          upholstery shop and spent a few hours 
                                          getting them put on. The old foam 
                                          padding was still useable although I 
                                          did have to add some foam to a few 
                                          places that had been eroded away. Now 
                                          I need to get some rear seat belts put 
                                          in. 
                                            
                                          
                                    July 24, 2004  I used the old,
                                          rotted wood from the rear seat as
                                          patterns to make a new seat back and
                                          bottom. After cutting out the wood, I
                                          coated the pieces with spar varnish
                                          and clear urethane to help protect it
                                          from moisture. I cleaned and sanded
                                          the seat frame and painted it with
                                          satin black. Then I took the remains
                                          of the original vinyl seat cover to an
                                          upholstery shop to be
                                          reproduced. 
                                           
                                     
                                           
                                    
                                    July 10, 2004  I had 
                                    determined that the original AM pushbutton 
                                    radio in the Scout was still good so I 
                                    ordered an OEM replacement 4x8 speaker to 
                                    replace the original which was completely 
                                    shot. Before I put the radio back in the 
                                    dash, I decided to run new defroster vent 
                                    hoses. I used Fresh Air-Defroster Duct Hose 
                                    from JC Whitney. In order to keep the hoses 
                                    securely in place I used 3M Super 
                                    Weatherstrip Adhesive. Getting access to the 
                                    dash area required the removal of my ABS 
                                    plastic glove box. There's not much room for 
                                    the defroster hoses to run behind the glove 
                                    box so I had to crush them a little to 
                                    provide space for the glove box. I checked 
                                    for air flow after attaching the hoses and 
                                    after reinstalling the glove box. I buttoned 
                                    everything back up and set one of the radio 
                                    presets to 1450 AM, our local oldies 
                                    station. 
                                           
                                      
                                    
                                    July 4, 2004  
                                    I decided to put 
                                    in my rear Prothane spring bushings. They 
                                    went a little easier than the front although 
                                    I had to cut out the upper rear bushings 
                                    that are in the frame brackets. 
                                      
                                    
                                    June 26, 2004  Today, I pulled 
                                    the passenger side gas tank, cleaned out 30 
                                    years worth of accumulated dirt in the body 
                                    cavity and installed the new filler hose I 
                                    got from SuperScout Specialists at AZIHR. I 
                                    also bought a Rancho 5000 shock to use as a 
                                    steering stabilizer. It makes the truck 
                                    harder to turn when you're not moving. I 
                                    think it might be too much for my manual 
                                    steering so I may take it off or go with a 
                                    regular el-cheapo shock that's not as stiff. 
                                      
                                    
                                    June 5-6, 2004  On the
                                    Gardner Canyon 
                                    trail run on May 23, I noticed the tie 
                                    rod was bent and the ball ends were badly 
                                    worn so this weekend I replaced the tie rod 
                                    and rebuilt the drag link ends. I had a new 
                                    tie rod and drag link repair kit from 
                                    SuperScout Specialists. When starting the 
                                    tie rod removal, it didn't appear that there 
                                    was enough ro om 
                                    to get the ball end shaft out of the spindle 
                                    without removing the front spring shackle. 
                                    Then, there still wasn't enough clearance to 
                                    drop the rod so I removed the rear shackle. 
                                    There still didn't look like there was 
                                    enough room to get the shaft out so I 
                                    loosened the u-bolt nuts so I could move the 
                                    spring around enough to get the tie rod end 
                                    off. After having almost removed the spri ng, 
                                    I decided to go ahead and put in the new 
                                    Prothane poly spring bushings I had gotten 
                                    several months ago. I used Harbor Freights
                                    
                                    3 in1 Service Tool Kit which works well 
                                    on spring bushings. Using its large C clamp, 
                                    I managed to push out 4 of the 6 spring 
                                    bushing intact. The other two I had to push 
                                    out the center sleeve and then saw out the 
                                    outer sleeve. After the old ones were out, I 
                                    put in the new poly bushings and reattached 
                                    the spring shackles with new grade 8 bolts. 
                                    The new tie rod went on easily and the 
                                    rebuilt drag link likewise. I used the 
                                    push-pin-in-the-center-of-the-tire method to 
                                    check and adjust toe-in to zero. After 
                                    everything was torqued to spec and lubed, I 
                                    took a turn around the block and was happy 
                                    to experience tighter, truer steering. 
                                      
                                    May 
                                    8-9, 
                                    2004  With temperatures in the
                                    mid to upper nineties already, I decided it
                                    was time to get the travel top off and
                                    stored away for the summer. In preparation
                                    for this, I needed to do some work on my
                                    spare tire carrier so I could get the tire
                                    out of the back of the Scout. I removed the
                                    rack and bent the legs so that they were a
                                    little more parallel to the tailgate. This
                                    allowed the 31x10.50 All Terrain tire to fit
                                    over the studs on the rack far enough so I
                                    could get lug nuts on them. It's a little
                                    off-center but hardly noticeable. 
                                    I
                                    also removed the rear seat. It's going to
                                    need new wood backing and vinyl covering and
                                    I might as well get 
                                    
                                     stared on that project
                                    too. The other thing I wanted to do was get
                                    the passenger side window to operate
                                    smoother. I removed the upholstered door
                                    panel and applied some white grease to the
                                    window regulator arms. Works a little
                                    better, but you still need to pull it up by
                                    hand while cranking. Guess I need to find a 
                                    new regulator. 
                                    The
                                    travel top was quite easy to get off. After
                                    removing, labeling and saving all the
                                    attachment bolts, my brother and I lifted
                                    off the top and set it on some 8"
                                    cinder blocks in the back yard. I might do
                                    some touch-up work on a couple of dents and
                                    replace the door window upper seals while
                                    it's off. 
                                    The
                                    Scout is like a whole 'nother vehicle with
                                    the top off! Lots cooler and less noisy
                                    without that metal acoustic chamber
                                    amplifying the road rattles and engine
                                    noise. I attached the bikini top that I got
                                    with the Scout from the PO. It's a little
                                    short in the back but it keeps the sun off
                                    my head and that's the main thing. Now, I'm
                                    anxious to take it out and do some topless
                                    cruising in the desert. 
                                    Things
                                    I need to consider are securing the Hi-Lift
                                    jack, as well as a camp shovel, come-a-long
                                    and various bungees I had stored under the 
                                    rear seat. I may need to mount some kind of 
                                    trail box securely to the floor that I can 
                                    lock stuff up in.  
                                      
                                    April
                                    24-25, 
                                    2004  Attended the 5th AZ IH
                                    Rendezvous in Prescott Valley, AZ. See the Trail
                                    Reports page for details. 
                                      
                                    March
                                    7, 
                                    2004  I successfully bid for a
                                    stock spare tire carrier on Ebay. I cleaned
                                    it up painted it satin black which I think
                                    is the original color. I mounted it to my
                                    tailgate and step bumper (that already had
                                    two of the mounting holes drilled in it).
                                    However, when I went to put my 31x10.50
                                    spare on it, there was not enough of the
                                    mounting surface extending out from the
                                    carrier to allow the wheel to contact it.
                                    The tire hits the tailgate and there's still
                                    a couple of inches left between the surface
                                    of the mount and the wheel. I'll have to
                                    figure out a way to either modify the mount
                                    for a deeper/larger tire or just continue to
                                    store my spare inside the Scout. Update: After
                                    looking closely at some other tire carriers,
                                    I seems mine is bent enough to prevent the
                                    tire from mounting properly. I'll need to
                                    remove it and bend it out straight again. 
                                      
                                    
                                    Feb 22, 
                                    2004  I've only had time to do
                                    some odds and ends on the Scout for the last
                                    couple of weeks. I put in the replacement
                                    glove box I got from ScoutParts.com.
                                    Fits perfect. I ordered some flexible air
                                    duct hose from JC
                                    Whitney Co to replace the defroster hose
                                    and the fresh air intakes. I received the 4
                                    1/2" hose for the engine compartment
                                    and put it on. When I receive the 2"
                                    hose for the defroster ducts, I'll need to
                                    pull out the glove box to get it installed
                                    though. 
                                    I
                                    also put on the Back
                                    Country Binders fuel filler flanges and
                                    new caps I had. This should keep the gas in
                                    the tanks when I go on the Sonora
                                    Desert Scouts trail run in March. I
                                    finished up by re-attaching the speedometer
                                    cable I had disconnected a couple weeks ago
                                    when I had the gauge panel off. 
                                    I
                                    successfully bid on a spare tire carrier on Ebay.
                                    I should be getting it in a week or so. 
                                      
                                    
                                    Feb 7, 
                                    2004  I finished up installing 
                                    the heater in the Scout. I lucked out and 
                                    found a  wire from the ignition switch 
                                    that had been cut off behind the dash. It 
                                    was right next to the heater fan switch so 
                                    it may have been used for that purpose 
                                    originally. I put a 14amp fuse on the line 
                                    and hooked it to the fan switch. After 
                                    reattaching the heater hoses and letting the 
                                    engine warm up a little, I tried everything 
                                    out and it works fine. 
                                      
                                    Feb
                                    1, 
                                    2004  Only had a little time
                                    to work on the Scout today before the Stupor
                                    Bowl started. I decided to put in the new
                                    driver's side wiper motor I got from  Chris
                                    in Colorado. I'll be driving the Scout to
                                    work this week and we're expecting the
                                    biggest winter storm of the season to hit on
                                    Tuesday. I wanted to make sure I can see
                                    where I'm going! I'm getting pretty good at
                                    R&Ring wiper motors now. The hardest
                                    part is getting the pin out of the knurled
                                    hub on the end of the wiper shaft. The rest
                                    is just a matter of getting the vacuum hoses
                                    on and off. 
                                    After
                                    that, I put on the new driver's side fuel
                                    filler neck I got from Scout
                                    M.A.D.ness in Lubbock, TX. I finished
                                    cleaning the sand and rocks out of the
                                    fender cavity next to the tank and put the
                                    rock guard/cover back on. I put a gallon of
                                    gas in the tank and switched the selector
                                    lever to the driver's side. I ran it long
                                    enough to tell me it was using gas from the
                                    driver's side tank so I filled it the rest
                                    of the way. 
                                    Thinking
                                    about the cold, wet weather we're supposed
                                    to get made me think of the heater that I
                                    had removed a month or so ago when I pulled
                                    out all the A/C stuff. I got some non-A/C
                                    ducts from Howie in N.Carolina. I cleaned up
                                    the parts and sprayed on a coat of satin
                                    black to match my dash. I checked out the
                                    heater core and put on the motor I got from
                                    Chris in Colorado to replace the bent
                                    squirrel cage on my original. I got the
                                    heater blower/core bolted back in the engine
                                    compartment but I'll need to tap a hot wire
                                    from the ignition switch for the heater
                                    blower switch and hook up the heat/vent cable
                                    before I can use it.  
									
                                    Jan 24, 
                                    2004  On my way home from a 
                                        Scout club meeting last week, I was 
                                        informed that my tail lights weren't 
                                        working. After half a day of tracing 
                                        wires and checking connections, removing 
                                        the tail light buckets, etc,  I 
                                        figured out that the turn signal 
                                        canceling cam I messed with on Jan 10 
                                        was the cause. Apparently, the switch is 
                                        still not making contact properly with 
                                        the turn signal harness. The lights work 
                                        fine when the left turn signal is on but 
                                        not when the turn signals are off. Looks 
                                        like I'll have to pull the steering 
                                        wheel again and make some more 
                                        adjustments. It's a cold, drizzly 
                                        weekend here in Tucson (our week of 
                                        winter) so I went inside to watch the  
                                        UofA Basketball game.   
									
                                    Jan 18, 
                                    2004  I focused on getting the 
                                        steering wheel back on so the Scout 
                                        would be driveable again. I guess I'll 
                                        have to wait to do a steering wheel 
                                        upgrade with a full install kit to get 
                                        the canceller to work. I decided to pull 
                                        the driver's side fuel tank to check it 
                                        for condition and rust. I have a new 
                                        filler neck on the way and wanted to 
                                        make sure the tank was OK before 
                                        installing it. I was very surprised at the condition of the tank. It almost 
                                        looked new! Just a couple of surface 
                                        rust spots on the outside. The inside 
                                        was clean with no sediment or rust. A
                                    P.O. had even taken the time to cover the
                                    fill tube opening with duct tape to keep the
                                    tank from collecting dirt and water. I 
                                        dabbed some  Eastwood Rust Encapsulator 
                                        on the rust spots, drilled out a 
                                        broken off tank mounting bolt and 
                                        reinstalled the tank. As is typical, the cavity next to 
                                        the tank was full of dirt. It's a good 
                                        thing we don't get much rain in Arizona, 
                                        because that could have really caused 
                                        some rust through if it had been allowed 
                                        to get wet very often.  I cleaned 
                                        it out and will install my new filler 
                                        neck next week. 
									
                                    
                                    Jan 10, 
                                    2004  I decided to pull the
                                    steering wheel and replace the turn signal
                                    canceling cam. As usual, a 2 hour job turned
                                    into a weekend project. I got the wheel off
                                    without trouble. The new canceling cam wires
                                    needed to be soldered to the old wires and
                                    following Murphy's Law, I hooked them up
                                    backwards. After fiddling with the contacts
                                    on the cam for an hour or so, I finally
                                    realized the wires may be crossed. After I
                                    swapped them, the turn signals worked again
                                    but there is nothing on the steering shaft
                                    or wheel hub to operate the canceling cam to make the
                                    signals shut off. So after a day's worth of
                                    work, I ended up no further ahead than I was
                                    before. Maybe I'll have better luck next
                                    weekend. 
                                      
                                    
                                    Jan 3-4, 
                                    2004  After some fun 
                                    4-wheeling in the snow up in the White 
                                    Mountains over Christmas (that's my son in 
                                    the photo, not me!), it was time to get 
                                    back to wo rk on the Scout. I decided to try 
                                    to fix the vacuum wipers but couldn't get to 
                                    the motors from under the dash. I removed 
                                    all the dash bolts and screws but then 
                                    realized the dash would only move about 2" 
                                    because the roll bar is in the way. Well, I 
                                    wasn't going to tear the whole scout apart, 
                                    so I removed the hubs on the shafts and then 
                                    the nut holding the shaft to the cowl. Lo 
                                    and behold, the motor fell out from the 
                                    inside. Turns out they are only held in 
                                    place by the shaft nut. I lubed up the 
                                    drivers side motor and checked it with a 
                                    vacuum source and it works ok. The passenger 
                                    side motor had a frozen shaft and I broke it 
                                    off trying to loosen it up. I'll have to 
                                    find another motor on  Ebay or the
                                     Binder
                                    Bulletin. I cleaned up the switches and ran 
                                    all new vacuum hoses. Buttoned up the dash 
                                    but I'll be back in there to do some wiring 
                                    work later.  
                                    
                                    Sunday, I put on 
                                    a step bumper I got from a guy in Colorado. 
                                    It's nice and beefy and looks better than 
                                    the stock chrome SR-2 bumper. The hardest 
                                    part was getting the bolts from the original 
                                    bumper off and bolting on the new brackets. 
                                    They are inside the frame rail and access is 
                                    pretty limited. Check out my new 
                                    personalized license plate. Cool, huh? 
                                      
                                    Dec
                                    20-21, 2003  I finally had an
                                    entire weekend to work on the Scout. I
                                    finished up the installation of the shifter
                                    and replaced the transmission tunnel. While
                                    I was cleaning the front floor pan area, I
                                    discovered some rust on the floors next to
                                    the rocker panels. Nothing that has rusted
                                    through yet though. I scraped off the loose
                                    flakes and coated the areas with Eastwood's 
                                    Rust Encapsulator. Once I pull up all the
                                    floor mats in the rear, I'm sure I'll find
                                    other similar spots. My intention is to
                                    eventually coat the entire inside floor area
                                    with POR-15 or
                                    RustBullet, but that's a whole 'nother
                                    project! 
                                    I
                                    replaced the 6ga positive battery cable with
                                    some new 1ga cable from Summit Racing. I
                                    took this opportunity to remove some unfused
                                    wiring the PO had running from the 
                                    positive battery cable to somewhere under
                                    the dash. Everything still worked after that
                                    so it must not have been anything important.
                                    I drained and refilled the transmission with
                                    fresh Dexron ATF. The old fluid was a
                                    greyish color so it was definitely in need
                                    of a change. I wasn't able to locate a
                                    transmission pan gasket so I didn't get to
                                    clean the filter. That will be on my list
                                    has soon as I can get a gasket. 
                                    
									Dec 
                                    14, 2003  I set aside the 
                                    whole day to install the replacement shifter 
                                    on the Borg Warner T-39 automatic transmission. 
                                    As usually happens with these kinds of 
                                    projects, a lot of unexpected things pop up 
                                    that take more time than originally 
                                    anticipated. I spent almost two hours 
                                    getting the floor mat up and 
										
                                     removing the 
                                    transmission tunnel bolts. I removed the 
                                    passenger seat and folded the mat over onto 
                                    the driver's side.  I got all but two cover bolts out 
                                    and then twisted the head off of one (it had 
                                    a bolt underneath  that held a clamp on the 
                                    shift cable) and another was rusted in place 
                                    and required the P B'laster treatment. Once 
                                    the cover was off I was finally able to see 
                                    exactly what I was dealing with. The 
                                    transmission heat exchanger is fully visible 
                                    and all the hose and trans fluid lines are
                                    accessible. The bracket that holds the 
                                    exchanger to the transfer case is severely 
                                    overbuilt. It is also in the way of mounting 
                                    the shifter plate brackets to the 
                                    transmission. I decided to remove that 
                                    bracket since there is adequate support from 
                                    the hoses and lines attached to the 
                                    exchanger. Besides, I'm planning to replace 
                                    it entirely with a flat plate exchanger in 
                                    the future.The instructions for installing 
                                    the shifter don't take into account that 
                                    there is a Dana 20 transfer case attached to 
                                    the rear of the transmission so I had to 
                                    make some allowances for that too. After 
                                    finally getting the shifter mounted and the 
                                    cable hooked up, it was late in the day and 
                                    I still need to cut a new hole in the cover 
                                    for the shifter handle. I also need to
                                    secure the shift cable farther away from the
                                    exhaust pipe and do something with the lock
                                    out switch. At least I now have a sturdy,
                                    firm shifter with a nice long handle. 
									
									
                                      
                                        
									
										Dec 7, 2003  I had intended to work on replacing the broken off shifter
                                        handle on the Borg Warner automatic transmission today. I
                                        had also received an alternator mounting bracket from an online purchase and wanted to get rid of the old combination A/C compressor/alt bracket. What I thought was going to be a simple job turned into a
                                        major effort. In order to remove the bolts from the old bracket, I had to remove the fan and water pump pulleys. Once that was done, I tried to test fit the new bracket. It bolted up fine to the head and a stud on the exhaust manifold. The only problem was that there was not enough room between the bracket and the inside fender well to get the alternator
                                        in! I had to grind down some webbing on the bracket and part of the alternator case to get enough clearance to
                                        even mount the alternator. This only gave me about 1/4 inch of adjustment though. After some precision work with a 5 lb sledge on the fender well sheet metal, I got about 1/2 in. of adjustment
                                        room. Then, after several trips to the auto parts store to get
                                        exactly the right length belt, I got the alternator mounted and the belt tightened and the fan put back in. By this time, I had spent three hours on what was supposed to take 30 minutes, so I decided to postpone the shifter
                                        work for yet another week. I took care of some other things that needed attention like lubing the front
                                        steering and reinstalling the dash pot on the carburetor.
                                        I discovered that the dash pot brackets
                                        on the rebuilt 2300 manual choke and the
                                        NOS 2300C are different lengths. I
                                        swapped them out so the 2300C will now
                                        idle down without snapping the throttle
                                        shut and stalling out. I decided to
                                        adjust the sagging door hinges so
                                        they'll be lined up nice when I replace
                                        the weather stripping. My PB'laster was
                                        put to use again on the stubborn door
                                        hinge bolts. I also put in a 1ga negative battery cable to replace the wimpy 4ga that was too long anyway. I'm going to do the same with the positive cable but I'll probably have to make up my own since 74" 1ga cables are not readily available. I was going to replace the door gaskets but ran out of time (again!). Little by little, things are getting done. Just wish I had more time work on them. 
									
										Nov 22, 2003  Finished up installing the new top seals today. They fit perfectly and seal out all the drafts I had been experiencing since I bought the Scout. With all the bolts in place, it also eliminates a lot of the rattles and squeaks. I think I'll do the door gaskets next so I'll have a completely
                                        weather tight ride this winter. 
									
                                        
									
										Nov 16, 2003  Got some new travel top seals from
                                         ScoutParts.com and got started putting them on. We do get some rain in Tucson during the winter and I want to make sure I have the Scout "dried in" before they start. I got the top off with the help of some old cable-type camper jacks I had. Those things are scary for lifting a cabover but they handle the travel top just fine. I went to Ace Hardware and got some 5/16 x 24
                                        flange bolts since the top is currently held on by only 3 bolts on each side. I got the top in the air and removed the remnants of the old seal and some kind of caulking that had been used on the windshield frame. Before I could get the new seals on, I had to go help my brother cut down some trees in his yard and haul a load to the dump. By the time I got home, there was only time to clean up before heading to the
                                         Scout Club meeting. I was going to drive the Scout topless but I couldn't get out from under the camper jacks. So I had to lower it back down and bolt it back on for now. Now that I've done it once, I should be able to get the seals on pretty quickly when I get some time. I still need to do something about that transmission shifter! 
									
										Nov 8, 2003  I saw a NOS Holley 2300 with automatic choke on Ebay, so I decided to replace the rebuilt 2300 manual choke which I hadn't been able to get running very well. Still had off-idle hesitation and was hard to start. I put on the 2300C and it made a world of difference! No more hesitation and starts right up.
                                        The only problem was that the dash pot
                                        doesn't allow the throttle to close far
                                        enough, even when adjusted all the way
                                        down. I removed it until I can figure
                                        out how to make it work. Now that I don't have to worry about the
                                        engine as much, I can focus on other things on the Scout. Next, I think I'll get the new door and top seals put on so I can stay dry when the winter rains come.  I mounted a pair of tow hooks on the frame horns under the front bumper and changed the fluid in the front diff. I still need to get the new shifter installed. Maybe in a couple of weeks. 
									
										Nov 2, 2003  I worked this weekend on getting the Scout to start and run better. I replaced the points and condenser and adjusted the timing. The $8 made-in-Taiwan distributor wrench I got at Checker was well worth the price. The distributor lock bolt is pretty inaccessible, especially with the A/C compressor bracket in the way. The timing was advanced quite a bit and I was getting stalling and backfiring from the carburetor when the throttle was opened fast off idle. Retarding the timing helped quite a bit. I don't know exactly how many degrees retarded it is because I didn't use a timing light. I just rotated the distributor until the idle came up and the stumble/backfire off idle went away. It still started ok so I don't think I retarded it too much. After I got it to run better, I took it for a spin on a nearby dirt lot and tested the operation of the transfer case in 4H and 4L. Everything seems to work.
  
									
                                        
									
										I decided to use the rest of my time to remove unwanted parts from the Scout. I started by yanking the York A/C compressor which a PO had already disconnected the hoses from. I discovered that the water pump, alternator and compressor are all driven by the same belt, which is adjusted by moving the compressor. So now I need to figure out a way to adjust the alternator to tighten the belt, which will be a lot smaller without the compressor in the loop. I'll probably have to fabricate some type of adjustable arm for the alternator if I don't replace the bracket altogether. Next, I removed the heater assembly from the engine compartment. I plan ro reinstall it after I have cleaned it up. I think it needs a new motor anyway. Besides the two bolts in the wheel well, there are 2 bolts holding the assembly to the firewall. One is easily accessed from the engine side. The other is tucked away under the dash behind the duct and blower motor for the dealer installed air conditioner. It was slow going trying to turn the nut 1/8 turn at a time and not being able to reach it with bare fingers. I don't know how it was put on to begin with, but I'll worry about that when the time comes to replace the heater.  
									
                                        
									
										Next, I removed the air conditioning condenser, blower and under dash unit from the cab. There's a lot more room under the dash and in the passenger side foot well now. This will make getting to the wiper motors and other stuff behind the dash
                                        much easier. 
									
										Oct 12, 2003  
                                        I was all ready with a list of projects 
                                        for the Scout so I got up bright and 
                                        early to get started. The first thing I 
                                        wanted to do was put on the rebuilt 
                                        Holley 2300 carburetor I had gotten from
                                         Checker
                                        Auto. When  I went to start the Scout to move it closer to the garage, the starter stuck and just kept turning over the engine which didn't want to fire. By the time I found a wrench to disconnect the battery, it had run it down to almost dead. I was worried about letting the starter motor run for what seemed like 5 minutes but it was probably only a couple. So after an hour and a half of fiddling with the starter switch and hooking up another battery, I finally got to the carb. Everything went pretty smoothly except I left out the 1/4" spacer that goes between the carb and the intake manifold thinking that all I needed was the gasket that came with the carb. Only trouble with that is that without the spacer, the accelerator pump gets pushed  up when you bolt down the carb. When I started the engine, it must have hit about 8000 rpm which is pretty high for any engine, let alone an IH V-8. Sounded like everything was going to come apart. Fortunately, it stalled pretty quickly but I did try it a couple more times before I figured out what the problem was. Nothing like abusing a 33 year old motor. Good thing it's an IH!  I had to hook up a cable since the new carb is a manual choke. I haven't figured out where to mount it on the dash so the cable just comes through the firewall and lies across the console for now.  
									
                                        
									
										I moved on to my next task which was changing the rear diff fluid. This went pretty well too and I verified that the D-44 is indeed a Powr-Lok after I got the cover off.  Before I forgot it, I mounted my 5 lb fire extinguisher to the roll bar on the driver's side. 
									
										My next project was to temporarily attach the spare tire behind the rear seat to keep it from rolling around. First, I had to mount the rear seat to the wheel well covers since it was just sitting loose in the back of the Scout. The 4 bolts were there and tightened down. Of course
                                        only 3 of them came out with little effort. The last one needed lots of
                                        PB'laster and vise grips to get it out. After the seat was secured, I cut some 2x6 scrap lumber to wedge the tire sideways and bungeed it to the seat back frame. That will suffice until I can fabricate a mounting bracket for the tailgate. By this time the day was pretty well over and I was getting tired anyway. I called it quits until the next time I get to work on it. 
									
										 Sept 16, 2003  I got my 800A Operator's Manual from
                                         Binder Books today. I read the instructions for shifting to 4L and it works fine! It's a two-handed operation that involves moving the transmission selector from D to R while pushing the transfer case lever up towards the 4L position. Not real intuitive. I never would have figured it out without the manual.   Sept 14, 2003  I decided to get the passenger side window back in so the neighborhood cats couldn't piss in the truck. I managed to reinstall the window regulator and secure it with 3 out of 4 screws. I still need a crank handle and a regulator clip but at least it keeps out the elements. I started to do some more in-depth checking of the truck. It turns out the TC145 (Dana 20) transfer case only shifts to 2H and 4H. It might just be that the linkage needs to be lubed. I was a few blocks from home when I tried it and didn't want to force it in case something broke and/or I got it stuck in N and couldn't get back home. I'll check into it more later. I took the truck to the neighborhood car wash and sprayed the engine and diffs. The grease is pretty well caked on so it didn't do much good. It's going to take some scraping and elbow grease to get it cleaned up good. I parked the truck and put a piece of cardboard underneath overnight. I didn't see any
                                        major
                                        drips the next day!  That's a good sign. At least there's no major oil leaks. I found that the
                                        wheel
                                        bolt pattern is the same as F**d light trucks/Br*nc*s. I have four of them lying around from a previous project, so I threw one in the back for a spare. Need to fabricate some kind of hold-down so it doesn't roll back and forth. I changed the oil and filter and called it good for the day.   Sept 10, 2003  Took the truck to get the title transferred. Had to go through ADEQ emissions testing first since it's a 1970 and the cutoff for exemption is 1966. I was a little worried but it passed OK! Went next door to the Arizona MVD and got my new plates and title. 
									
										As purchased September 9, 2003 
									
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